0% found this document useful (0 votes)
12 views9 pages

Bad Actor RCFA Gas Export Compressor K7230 Dry Seal Leak

The RCFA investigates a dry gas seal leak in Plant-B Export Compressor K7230, resulting in a production loss of 1.37 Kb/d over five months and an estimated repair cost of USD 1.5 million. The analysis will cover mechanical, operational, and maintenance histories, as well as human factors and recommendations for reliability improvements. A structured methodology involving data collection, failure mode analysis, root cause identification, and verification will be employed to address the issue.

Uploaded by

Jerome LIKIBI
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as PDF, TXT or read online on Scribd
0% found this document useful (0 votes)
12 views9 pages

Bad Actor RCFA Gas Export Compressor K7230 Dry Seal Leak

The RCFA investigates a dry gas seal leak in Plant-B Export Compressor K7230, resulting in a production loss of 1.37 Kb/d over five months and an estimated repair cost of USD 1.5 million. The analysis will cover mechanical, operational, and maintenance histories, as well as human factors and recommendations for reliability improvements. A structured methodology involving data collection, failure mode analysis, root cause identification, and verification will be employed to address the issue.

Uploaded by

Jerome LIKIBI
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as PDF, TXT or read online on Scribd

1

BAD ACTOR RCFA:


PLANT-B EXPORT COMPRESSOR K7230 DRY GAS SEAL LEAK
CAUSING PRODUCTION LOSS OF 1.37Kb/d FOR 5 MONTHS AND REPAIR COST ESTIMATED
USD 1.5 MILLION

Scope
The RCFA aims to identify the root causes and contributing factors behind the dry gas seal
leak on the Plant-B Export Compressor K7230, which led to:
▪ A production loss of 1.37 Kb/d over 5 months
▪ An estimated repair cost of USD 1.5 million
▪ Multiple failed restart attempts and eventual rotor seizure
2

This analysis will cover:


• Mechanical, operational, and maintenance history of K7230
• Seal system design, instrumentation, and failure modes
• Human factors, including troubleshooting and decision-making timelines
• Recommendations to prevent recurrence and improve system reliability
• Recommendations to prevent recurrence and improve system reliability
Methodology
The RCFA will follow a structured, multidisciplinary approach using the following tools and
techniques:
1. Data Collection
▪ Incident timeline reconstruction (from 6 August to 15 September 2025)
▪ Review of DCS/SCADA logs, alarm history, and trip records
▪ Maintenance and inspection records of K7230 and seal system
▪ Vendor reports and AGTS troubleshooting notes
▪ Interviews with operations, maintenance, and reliability teams
2. Failure Mode Analysis
▪ Apply Failure Modes and Effects Analysis (FMEA) on dry gas seal system
▪ Evaluate potential causes: contamination, misalignment, pressure imbalance,
thermal distortion, etc.
▪ Cross-reference with OEM design tolerances and operating envelopes
3. Root Cause Identification
▪ Use logic tree and 5-Why analysis to trace failure pathways
▪ Apply Apollo or TapRooT® methodology to distinguish root vs. contributing causes
▪ Assess human and organizational factors (e.g., delayed shutdown, troubleshooting
gaps)
4. Verification and Validation
▪ Correlate findings with physical evidence (e.g., rotor condition, seal wear patterns)
▪ Compare with similar incidents (internal or industry-wide)
▪ Validate hypotheses with subject matter experts (SMEs)
Testing and Diagnostic Plan
To support the RCFA and future reliability improvements, the following testing and
diagnostics are proposed:
A. Seal System Integrity Testing
▪ Dry gas seal leakage test (inboard/outboard)
▪ Seal gas flow and pressure differential verification
▪ Nitrogen purge and buffer gas system checks
3

B. Rotor and Bearing Inspection


▪ Runout and alignment checks
▪ Journal and thrust bearing wear analysis
▪ Vibration signature review (pre- and post-failure)
C. Instrumentation and Control Loop Testing
▪ Calibration of LHH63HSD-HPC and related transmitters
▪ Functional testing of trip logic and permissive interlocks
▪ Review of seal vent pressure control loop tuning
D. Contamination and Oil Analysis
▪ Lube oil and seal gas sample analysis for particulates or hydrocarbons
▪ Breather oil path tracing to identify ingress routes
PLANT -B K7230 COMPRESSOR DATASHEET
4

Background of Incident
▪ Plant-B Train 2 (K7230) experience trip on LHH63HSD-HPC Primary Seal Vent Pressure
Discharge Side High SDL on the 6th August 2025 approximately at 2200 hours
▪ Few starts attempted but unsuccessful as the unit keep-on tripping on the same
indication
▪ At the last attempt unit was restarted successfully and during warm-up sequence it
was observed heavy oil flow from the HPC Discharge Side journal breather
▪ Manually down the compressor for troubleshoot
▪ Troubleshoot by AGTS 11thAugust – 19thAugust.
▪ RG initial plan for rectification from 19th August – 2nd September but found the
compressor rotor unable to rotate.
▪ The compressor has been sent to shore on 15th September for rectification.
5
6
7
8
9

You might also like