0% found this document useful (0 votes)
40 views43 pages

Chem Cleaning

The document discusses the process of chemically cleaning the boiler units at a power plant. It involves removing internal deposits from the boiler using alkali boil out and acid pickling procedures. The alkali boil out uses chemicals like sodium phosphates to loosen deposits, while acid pickling uses an acid solution to remove remaining deposits and establish a protective layer.
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as PPT, PDF, TXT or read online on Scribd
0% found this document useful (0 votes)
40 views43 pages

Chem Cleaning

The document discusses the process of chemically cleaning the boiler units at a power plant. It involves removing internal deposits from the boiler using alkali boil out and acid pickling procedures. The alkali boil out uses chemicals like sodium phosphates to loosen deposits, while acid pickling uses an acid solution to remove remaining deposits and establish a protective layer.
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as PPT, PDF, TXT or read online on Scribd
You are on page 1/ 43

POST OPERATIONAL

CHEMICAL CLEANING
OF
UNIT#1 BOILER
A DUTTA
RAJIB GHOSH
VINAY JAISWAL
WHAT IS CHEMICAL CLEANING

REMOVAL OF INTERNAL DEPOSITS INSIDE THE


BOILER i.e.-WATER CIRCUIT WHICH INCLUDES,
ECONOMISER, DRUM ,DOWNCOMERS,WATER
WALL AND RISER TUBES BY TREATEMENT WITH
CHEMICALS AND THEN AGAIN ESTABLISHING THE
PROTECTIVE LAYER.
.
CHEMICAL CLEANING
WHY

 FOR NEWLY SUPPLIED BOILER TO WASH THE DEPOSITS,


WELDFLESH CORROSION AND OIL,GREASE ETC CHEMICAL
CLEANING IS RECOMMENDED.

 FOR BOILER IN USE FOR MANY YEARS, THE SCALES,


CORROSIVE SALTS, SILCATES AND CARBONATES ARE
DEPOSITED IN BOILER WHICH HAMPERS THE HEAT TRANSFER.

 THESE DEPOSITS MAY INCREASE METAL SURFACE


TEMPERATURE AS THE THERMAL CONDUCTIVITY OF SALTS ARE
VERY POOR-RESULTING IN TUBE FAILURE.
OVERHEATING OF TUBE DUE TO
INTERNAL OXIDE/DEPOSITION
Increase in metal temperature due
to internal scale

FACTORS INFLUENCING DEPOSIT IN
BOILER TUBES.
• NUMBER OF STARTUPS / SHUTDOWN

• INGRESS OF RAW WATER FROM CONDENSER


LEAKAGES OR SEEPAGES.
• CHANGE IN FEED / MAKEUP WATER QUALITY
• CRUD FORMATION DUE TO CORROSION AT LP SIDE
AND TRANSFER TO THE BOILER.
• BOILER WATER CHEMISTRY DEVIATIONS
• PRESERVATION OF BOILERS DURING IDLE PERIOD
• BOILER CYCLE METALLURGY
REMEDIAL MEASURES

• PERIODIC POST OPERATIONAL ACID CLEANING OF


BOILERS TO REMOVE THE EXISTING INTERNAL
OXIDE LAYER AND FORMATION OF PROTECTIVE
MAGNETITE LAYER.
• MAINTAINING BOILER WATER PARAMETERS
STRICTLY
• CONTROL THE INGRESS OF IMPURITIES I.E.
COOLING WATER THROUGH CONDENSER, WHICH
WILL REDUCE THE PHENOMENA OF SALT
CONCENTRATION BY “WICK BOILING”.
CHEMICAL CLEANING
BASIS FOR UNIT-1 CHEMICAL CLEANING

INTERNAL DEPOSIT QUANTITY AS PER R&D LAB

S.NO MONTH/YEAR HOT SIDE, mg/cm2 COLD SIDE mg/cm2


.
1 05/2005 22-66 10-60

2 10/2005 22-50 14-28


FACTORS AFFECTING THE ACID
CLEANING PROCESS
• QUANTITY OF INTERNAL DEPOSIT IN WATERWALL
TUBES.
• QUALITY/ANALYSIS OF DEPOSIT.
• SELECTION OF PROPER SOLVENT.
• SELECTION OF ACID INHIBITOR AND PERCENTAGE
INHIBITION DURING THE PROCESS.
• TEMPERATURE OF THE SOLUTION DURING THE
PROCESS.
• CIRCULATION SPEED AND CONTACT TIME.
• ANALYSIS OF SOLVENT DURING THE PROCESS AND
COMPLETION CRITERIA.
CHEMICAL CLEANING
PROCEDURES

 ALKALI BOIL OUT

 ACID PICKLING

 NEUTRALIZATION

 PASSIVATION
CHEMICAL CLEANING
ALKALI BOIL OUT

 TO DISLODGE / LOOSENING OF HARD, ADHERENT


DEPOSIT ON THE INTERNAL SURFACES OF TUBE

 CHEMICAL USED: TRISODIUM PHOSPHATE (1000 PPM) AND


DISODIUM PHOSPHATE (500 PPM)
CHEMICAL CLEANING
ALKALI BOIL OUT PROCEDURE
 BOILER DRUM FILLED UPTO BOTTOM LEVEL & CHEMICALS
CHARGED THRU DRUM MAN HOLE

 BOILER IS LIGHTED UP & PRESSURE IS RAISED UPTO ¼


RATED PR. WITH NORMAL DRUM LEVEL

 HOLD THE PRESSURE FOR 2 HRS AND BLOW DOWN IS


GIVEN THRU LOW POINT DRAINS IN SEQUENCE EACH FOR
30 SECONDS, AFTER THE FIRE IS PUT OUT.
CHEMICAL CLEANING
ALKALI BOIL OUT PROCEDURE
 THE PROCESS OF RAISING PRESSURE, HOLDING PRESSURE AND
BLOW DOWN ARE REPEATED FOR SIX TIMES.

 THE SAMPLES ARE ANALYSED FOR PH AND ALKALINITY


MEASUREMENT.

 DEPRESSURIZE THE BOILER DRUM UPTO 2 KG/CM2, THEN ENTIRE


SYSTEM IS DRAINED HOT.

 ON COMPLETION OF TOTAL DRAINING, THE BOILER IS WASHED


WITH DM WATER TILL THE DRAIN SAMPLE IS FREE FROM
PHOSPHATE.
RESULTS OF BOILER ALKALI BOILOUT SAMPLES:
Time ph Phosphate Grease/oil Total alkality Silica (ppm)
(ppm) (ppm)
03:05Hrs 11.2 22.6 Traces 732 4.0
05:15Hrs 11.5 2500 Not detectable 880 1.1

07:30Hrs 11.0 1750 Not detectable 860 <1

09:50Hrs 11.2 1560 Not detectable 768 <1

12:15Hrs 11.0 1430 Not detectable 700 <1

14:00Hrs 10.8 1250 Not detectable 708 <1

14:50Hrs 11.0 1250 Not detectable 684 <1

RESULTS OF BOILER RINSING SAMPLES:

Sample No. ph Phosphate in ppm Conductivity


1st --- 0.8 ---
2nd --- 50 150
3rd --- 2.19 12
4th --- 12 22
5th 7 0.5 1
6th 7 0.3 0.5
7th 7 0.7 0.6
CHEMICAL CLEANING
ACID PICKLING PREPARATION
 DRUM INTERNALS REMOVAL

 INSTALLING ORIFICE PLATE IN ALL DOWNCOMER

 ISOLATE SUPERHEATER BY PLUGGING THE CONNECTING


TUBES FROM DRUM TO SUPER HEATERS.

 THE ERECTION OF TEMPORARY PIPING, VALVES, FITTINGS,


CIRCULATION TANK AND PUMPS
 Schematic diagram for boiler chemical cleaning
CHEMICAL CLEANING
CHEMICAL CLEANING
ACID PICKLING PREPARATION
SUPERHEATER FILLING:

• BACK FLUSH THE SUPERHEATER WITH DM WATER

• BACKFILL THE SUPERHEATER WITH TREATED WATER


CONTAINING 200-PPM HYDRAZINE AND AMMONIA TO PH 10.

• PLUG THE SUPERHEATER CONNECTING TUBES INSIDE THE


DRUM.

• RAISE THE PRESSURE TO 4-5 KG/CM2 (G) AND ISOLATE THE


SUPERHEATER.
CHEMICAL CLEANING
SUPER HEATER CIRCUIT BACK FLUSHING CHEMICAL REPORT :

DATE SAMPLING TIME PO4 ph TURBIDITY

09.10.07 00:30Hrs 0.2 ppm 6.7 Clear

09.10.07 00:45Hrs 0.2 ppm 6.7 Clear

SUPER HEATER CIRCUIT BACK FILLING CHEMICAL REPORT:

DATE SAMPLING TIME ph HYDRAZINE (N2H4) IN PPM


09.10.07 09:00Hrs 10.00 424
09.10.07 10.20Hrs 10.00 480
09.10.07 12.10Hrs 10.00 408
09.10.07 13.20Hrs 10.00 480
09.10.07 14.30hrs 10.00 640
09.10.07 15.30Hrs 10.00 480
09.10.07 16.30Hrs 10.00 464
16:30 Hrs : Super Heater vent samples
CHEMICAL CLEANING
ACID PICKLING PREPARATION
COLD WATER RINSE:

FILL THE SYSTEM WITH DM WATER AND ESTABLISH


CIRCULATION BY PUMPS. CIRCULATE FOR ABOUT ½ AN
HOUR AND DRAIN.

HOT WATER RINSE:

FILL THE SYSTEM WITH DM WATER OF TEMPERATURE 55-60


ºC BY PASSING THE STEAM IN THE CIRCULATING TANK AND
ESTABLISH CIRCULATION BY PUMPS AND DRAIN AFTER
CIRCULATION OF HALF AN HOUR.
CHEMICAL CLEANING
HOT WATER RINSING LOG:

DATE TIME INLET PR. INLET TEMP OUTLET PR OUTLET TEMP TURBIDITY

10.10.07 01:45Hrs 7.5 48 7.5 28 ---


10.10.07 02:15Hrs 7.0 68 7.0 28 ---
10.10.07 02:45Hrs 7.5 68 7.5 29 ---
10.10.07 03:15Hrs 7.0 68 7.0 32 ---
10.10.07 03:45Hrs 6.7 70 6.7 40 3 NTU
10.10.07 04:15Hrs 6.0 80 6.0 46 ---
10.10.07 04:45Hrs 6.0 80 6.0 48 3 NTU
10.10.07 05:15Hrs 7.0 86 7.0 54 ---
10.10.07 05:45Hrs 7.0 92 7.0 58 3 NTU
10.10.07 06:15Hrs 6.0 86 6.0 60 ---
10.10.07 06:45Hrs 6.5 88 6.5 62 ---
10.10.07 07:30Hrs 6.5 88 6.5 66 ---
CHEMICAL CLEANING
ACID PICKLING PROCEDURE
 THE FOLLOWING CHEMICALS ARE REQUIRED FOR ACID
PICKLING STAGE:

1. ACID INHIBITOR: 0.20% (v/v)


2. AMMONIUM BIFLUORIDE: 0.25% (w/v)
3. THIOUREA: 1.0% (w/v)
4. HYDROCHLORIC ACID: 5.0% (w/v)
CHEMICAL CLEANING
ACID PICKLING PROCEDURE
 FILL THE BOILER WITH DM WATER AND ESTABLISH
CIRCULATION WITH PUMPS.

 ADMIT STEAM INTO MIXING TANK AND RAISE THE


TEMPERATURE OF CIRCULATING WATER TO ABOUT 65 ºC IN
RETURN LINE.

 CUT OFF STEAM AND ADD REQUIRED QUANTITY OF ACID


INHIBITOR (CORONIL).

 KEEP THE PUMPS RUNNING FOR THOROUGH MIXING.


CHEMICAL CLEANING
ACID PICKLING PROCEDURE
 CHARGE CALCULATED QUANTITY OF AMMONIUM BIFLUORIDE IN THE
MIXING TANK SLOWLY AND CIRCULATE THE SYSTEM FOR COMPLETE
MIXING OF CHEMICAL.

 ADD REQUIRED QUANTITY OF THIOUREA INTO THE CIRCULATION


TANK AND CIRCULATE THE SYSTEM FOR COMPLETE MIXING OF
CHEMICALS.

 ADD REQUIRED QUANTITY OF HCL IN CONTROLLED MANNER SO


THAT ACID CONCENTRATION DOES NOT INCREASE MORE THAN 6%.
CHEMICAL CLEANING
ACID PICKLING PROCEDURE
 ACID CONCENTRATION IS TO BE MEASURED AT THE INTERVALS
OF 10 MINUTES WHILE THE ACID IS BEING ADDED.

 ANALYSE THE SAMPLES FROM INLET AND RETURN LINE FOR ACID
CONCENTRATION, IRON AND COPPER.

 THE CIRCULATION WILL BE TERMINATED ONCE STEADY READINGS


OF IRON, COPPER AND ACID ARE OBTAINED IN BOTH INLET AND
RETURN LINES AND MAXIMUM SIX HOURS AFTER ADDITION OF
CHEMICALS. DRAIN THE SYSTEM UNDER NITROGEN CAPPING.
TIME OUTLET OUTLET
CHEMICAL CLEANING
SH PR. VENT ACID ACID % Fe IN Fe OUT Cu IN Cu OUT
(Hrs) PR. TEMP O/F % IN OUT (ppm) (ppm) (ppm) (ppm)
15:25 5.5 66 11/5 NO 1.9 --- --- --- --- ---
15:40 5.5 66 11/5 NO 0.8 --- --- --- --- ---
15:55 5.5 66 11/5 NO 4.6 --- --- --- --- ---
16:10 5.5 66 11/5 NO 3.7 --- --- --- --- ---
16:25 5.5 66 11/5 NO --- 1.8 --- --- --- ---
16:35 5.5 66 11/5 NO 4.5 --- --- --- --- ---
16:50 6.0 66 11/5 NO 5.0 --- --- --- --- ---
17:00 6.0 66 11/5 NO --- 3.0 --- --- --- ---
17:10 6.0 66 11/5 NO 5.9 3.4 --- 6423 --- ---
17:20 6.0 66 11/5 NO 5.1 --- --- --- --- ---
17:25 6.0 66 11/5 NO --- 4.7 --- --- --- ---
17:40 6.0 64 11/5 NO 4.7 4.6 7987 6981 --- ---
18:25 6.5 62 11/5 NO 6.4 --- --- --- --- ---
18:30 7.0 62 11/5 YES --- 3.8 9103 6936 --- ---
18:45 7.0 62 11/5 YES --- 4.5 --- --- --- ---
19:00 7.0 62 11/5 YES 5.3 4.8 9047 9103 --- ---
19:15 7.0 62 11/5 YES 4.4 4.4 --- --- --- ---
19:30 7.0 61 11/5 YES 5.6 4.5 8936 9550 --- ---
19:45 7.0 61 11/5 YES 6.5 4.5 --- --- --- ---
20:00 7.0 61 11/5 YES 6.5 5.4 10000 9550 133 133
20:00 7.0 61 11/5 YES 6.5 5.4 9885 10053 --- ---
20:30 7.0 60 11/5 YES 6.5 5.4 10000 9550 133 133
20:45 7.0 60 11/5 YES --- --- 9932 9885 --- ---
21:00 7.0 60 11/5 YES --- --- 10000 9550 133 133
CHEMICAL CLEANING
DM WATER RINSE:

 FILL THE SYSTEM WITH DM WATER

 ESTABLISH CIRCULATION. INCREASE THE TEMPERATURE OF


WATER UPTO 50-60 ºC BY INJECTING STEAM

 CIRCULATE FOR 30 MINUTES.

 DRAIN THE SYSTEM UNDER NITROGEN CAPPING.


CHEMICAL CLEANING
DM WATER RINSING LOG:
TIME INLET PR. INLET OUTLET PR. OUTLET SH PR. VENT Fe OUT pH
(Hrs) TEMP TEMP O/F (ppm)

23:30 7.0 80 2.2 52 11/5 NO --- ---

00:00 7.0 85 5.0 52 11/5 NO --- ---

00:30 7.0 85 5.5 52 11/5 NO --- ---

01:00 7.5 84 7.2 54 11/5 YES --- ---

01:30 7.7 82 7.5 55 11/5 YES --- ---

02:00 7.3 75 7.0 56 11/5 YES --- ---

02:40 7.6 78 6.0 58 11/5 YES 1955 3.5


CHEMICAL CLEANING
CITRIC ACID RINSE:

FILL THE SYSTEM WITH DM WATER AND ESTABLISH
CIRCULATION.

• RAISE THE TEMPERATURE OF CIRCULATING WATER TO


50-55 ºC AND ADD 0.2% (W/V) CITRIC ACID.

• ADD LIQUOR AMMONIA TO RAISE THE PH OF THE


CIRCULATING WATER TO 3-5-4.0.

• CIRCULATE FOR 2 HOURS. MEASURE THE PH AND IRON


CONTENT IN THE SOLUTION AT THE INTERVAL OF ½ AN
HOUR.

• DRAIN THE SYSTEM UNDER NITROGEN CAPPING.


CHEMICAL CLEANING
CITRIC ACID RINSING LOG:
TIME INLET INLET OUTLET OUTLET SH PR. VENT Fe IN Fe OUT pH pH
(Hrs) PR. TEMP PR. TEMP O/F (ppm) (ppm) IN OUT

06:30 6.0 76 0 45 11/5 NO --- --- --- ---

07:00 6.0 76 2.5 45 11/5 NO --- --- --- ---

07:30 6.0 64 5.0 44 11/5 NO --- --- --- ---

08:00 7.2 62 6.5 46 11/5 YES --- --- --- ---

08:30 7.6 65 7 48 11/5 YES --- --- --- ---

09:00 7.6 75 7 55 11/5 YES 559 559 3.2 3.2

09:30 7.0 75 6.5 55 11/5 YES 559 559 3.5 3.5

10:00 7.0 78 6.5 58 11/5 YES 559 559 3.5 3.5

10:30 7.0 80 6.5 60 11/5 YES 559 559 3.5 3.5

11:00 6.5 70 6 62 11/5 YES 559 559 3.5 3.5


CHEMICAL CLEANING
1ST & 2ND DM WATER RINSE:

 FILL THE SYSTEM WITH DM WATER AND ESTABLISH


CIRCULATION.

 RAISE THE TEMPERATURE OF CIRCULATING WATER TO


50-55 ºC AND CIRCULATE FOR ½ AN HOUR.

 MEASURE THE IRON IN THE INLET AND RETURN LINE


SOLUTION.

 DRAIN THE SYSTEM UNDER NITROGEN CAPPING.


REPEAT THE SAME PROCEDURE AGAIN.
CHEMICAL CLEANING
NEUTRALISATION:
 FILL THE SYSTEM WITH DM WATER AND ESTABLISH
CIRCULATION.

 ADD 0.5% OF SODA ASH IN THE CIRCULATING TANK TO


NEUTRALIZE THE SYSTEM.

 RAISE THE TEMPERATURE OF CIRCULATING WATER TO 80-


85 ºC BY ADDITION OF STEAM AND CIRCULATE FOR 6
HOURS.

 MEASURE THE PH IN THE INLET AND OUTLET OF SAMPLES.

 DRAIN THE SYSTEM WITHOUT NITROGEN CAPPING.


CHEMICAL CLEANING
1ST DM WATER RINSING LOG:
TIME INLET INLET OUTLET OUTLET SH VENT Fe IN Fe OUT pH pH
(Hrs) PR. TEMP PR. TEMP PR. O/F (ppm) (ppm) IN OUT

13:30 6.5 80 1.0 50 11/5 NO --- --- --- ---

14:00 6.5 65 4.5 54 11/5 NO --- --- --- ---

14:20 6.5 60 5.0 56 11/5 NO --- 34 --- ---

14:30 6.5 64 5.0 64 11/5 NO 25 25 5 5

14:45 --- --- --- --- 11/5 NO --- 55 --- ---

15:00 6.5 64 5.0 60 11/5 NO --- 50 --- ---

15:30 7.0 63 6.5 56 11/5 YES 25 55 6 5

16:00 6.5 67 6.0 56 11/5 YES 23 23 5 5


CHEMICAL CLEANING
2nd DM WATER RINSING & NEUTRALIZATION LOG:
TIME INLET PR. INLET OUTLET PR. OUTLET SH PR. VENT Fe OUT pH IN pH OUT
(Hrs) TEMP TEMP O/F (ppm)

18:30 6.0 40 2.5 52 11/5 NO --- --- ---

19:00 6.0 72 6.0 50 11/5 NO --- --- ---

19:30 7.0 82 6.5 38 11/5 YES 20 --- ---

20:00 7.0 72 6.5 52 11/5 YES --- 10.5 10.5

20:30 7.0 87 6.5 52 11/5 YES --- 10.5 10.5

21:00 7.0 87 6.5 54 11/5 YES --- 10.5 10.5

21:30 7.0 90 6.5 62 11/5 YES --- 10.5 10.5

22:00 7.0 95 6.5 65 11/5 YES --- 10.5 10.5

22:30 7.0 95 6.5 70 11/5 YES --- 10.5 10.5

23:00 7.0 98 6.5 72 11/5 YES --- 10.5 10.5


CHEMICAL CLEANING
PASSIVATION STAGE–I:

• FILL THE SYSTEM WITH DM WATER AND ESTABLISH


CIRCULATION.

• ADD HYDRAZINE TO GET THE CONCENTRATION OF 400 – 500 PPM


AND ADD AMMONIA SOLUTION TO RAISE THE PH UPTO 10.0.

• RAISE THE TEMPERATURE OF SOLUTION UPTO 80-90 C BY


ADDITION OF STEAM AND CIRCULATE FOR 20 HOURS.

• MEASURE THE HYDRAZINE CONCENTRATION AND PH OF


CIRCULATING WATER PERIODICALLY. ADD THE HYDRAZINE INTO
THE SOLUTION WHEN THE CONC. GOES BELOW 200 PPM.

• DRAIN THE SYSTEM IN HOT CONDITION. OPEN VENT, DRUM


MANHOLES AND CUT BOTTOM RING HEADER STUBS TO COOL
DOWN THE SYSTEM IN AERATED CONDITION.
CHEMICAL CLEANING
1st STAGE PASSIVATION LOG:
TIME (Hrs) INLET INLET OUTLET OUTLET SH VENT N2H4 IN N2H4 OUT pH pH
PR. TEMP PR. TEMP PR. O/F (ppm) (ppm) IN OUT

01:00 7.0 80 2.0 40 11/5 NO --- --- --- ---


01:30 7.0 84 5.5 40 11/5 NO --- --- --- ---
02:00 7.0 90 6.5 62 11/5 YES --- --- 10.5 10.5
03:00 7.5 94 7.0 66 11/5 YES --- --- 10.5 10.5
04:00 7.5 97 7.0 70 11/5 YES 376 272 10.5 10.5
05:00 8.0 98 7.5 72 11/5 YES --- --- --- ---
06:00 7.9 95 7.6 74 11/5 YES 328 336 10.5 10.5
07:00 7.8 96 7.5 76 11/5 YES --- --- --- ---
08:00 7.8 96 7.5 76 11/5 YES 376 392 10.5 10.5
09:00 8.0 96 7.5 77 11/5 YES --- --- --- ---
10:00 8.0 94 7.5 77 11/5 YES 352 360 10.5 10.5
11:00 8.0 92 7.7 77 11/5 YES --- --- --- ---
12:00 7.8 92 7.0 78 11/5 YES 336 352 10.5 10.5
13:00 7.8 92 7.0 78 11/5 YES --- --- --- ---
14:00 7.5 90 6.5 78 11/5 YES 320 336 10.5 10.5
15:00 7.5 92 6.8 80 11/5 YES 312 312 10.5 10.5
CHEMICAL CLEANING
PASSIVATION STAGE–II:

 RESTORE THE BOILER AFTER CHEMICAL CLEANING BY PUTTING DRUM


INTERNAL AND ALL THE PERMANENT CONNECTIONS.

 PREPARE THE BOILER FOR REGULAR OPERATIONS AS PER THE


GUIDELINES OF O&M.

 FILL UP THE BOILER WITH DM WATER CONTAINING 200 PPM OF


HYDRAZINE AND AMMONIA TO RAISE PH 10.

 LIGHT UP THE BOILER AND RAISE THE PRESSURE TO 40 KG/CM2 AND


MAINTAIN THE PRESSURE FOR 24 HOURS.

 DURING THE PROCESS, INJECT HYDRAZINE IN THE FEED WATER TO


MAINTAIN HYDRAZINE CONCENTRATION 200 PPM.

 AFTER COMPLETION OF II STAGE PASSIVATION, THE BOILER CAN BE


TAKEN UP FOR NORMAL OPERATION.
CHEMICAL CLEANING
2nd STAGE PASSIVATION LOG:

TIME (Hrs) BOILER WATER FEED WATER STEAM CONDENSATE


pH N2H4 (ppm) pH N2H4 (ppm) pH N2H4 (ppm) pH N2H4 (ppb) COND

23:00 10.5 40 ---- ----- ---- ----- ---- ---- ----

00:40 10.5 104 10.5 120 10.5 128 ---- ---- ----

03:00 ---- ----- ---- ----- ---- ----- 6.8 ---- 1.2

05:00 10 40 ---- ----- ---- ----- ---- ---- ----

06:30 ---- ----- ---- ----- ---- ----- 6.0 10 1.6

11:15 10 96 10 208 10 224 7.5 14 7.5

15:10 10 120 ---- ---- 10 256 6.5 10 6.2


CHEMICAL CLEANING
EFFICIENCY IMPROVEMENT DUE TO
CHEMICAL CLEANING OF UNIT NO.1

Parameter Unit Design Before After Change


Value O/H O/H
Flue Gas ºC
Temp.
Boiler %
Efficiency
Unit Heat Kcal/
Rate KWH
CHEMICAL CLEANING
LEARNINGS
 BOILER FILL P/P LINE FOR S/H FILLING HEALTHINESS
TO BE ENSURED BEFOREHAND
 CHEMICALS AVAILAIBILITY AND PURITY OF N2
CYLINDERS TO BE CHECKED BEFORE HAND
 SUPERHEATER CIRCUIT VALVES HEALTHINESS TO BE
ENSURED
 TEMPORARY PUMPS TRIAL TO BE INITIATED EARLY.
THANK YOU

You might also like